A friend got the job of moving a large laser cutting machine from Brisbane to Sydney, and being at least a two person job I went along to help.
It’s about 7m by 4.5m with a cutting area of about 6m by 4m. It’s designed for cutting fabric for making blinds, and the cutting table has a vacuum system to hold the fabric in place.
This is how it looked when we arrived:

Due to its size it wasn’t possible to move it in one piece, so we basically had to dismantle the the entire thing, taking plenty of photos along the way!
The first step though was to make sure it actually worked before we took it apart - especially the LASER itself:

Testing the laser involved wiring up power as some of the leads had been cut, and working out how to get the control software to fire it.
Since we didn’t have a compressed air supply it wasn’t safe to run the laser through the machine’s optics (the very expensive lens can be overheated without the cooling air) so we put some tape on a steel ruler and sat it in front of the laser’s ouput hole. Firing the laser left a nice burn hole in the tape, so it was definitely working!

After the laser test, it was time to pull everything apart.
The whole machine was bolted together fortunately, so we didn’t have to cut anything. There were a lot of bolts though, and some of them were damaged due to the machine being dragged across the floor previously.

This photo shows the vacuum trays which are under the mesh surface of the table (which is held on with seemingly millions of small screws!)
The divider plates in the middle can move back and forward to section off the vacuum to the area where it’s required.

Here are two sides of the frame remaining while the last of the vacuum trays are removed by forklift.

All the parts took up an entire semi trailer, and a ute!
After a few days off while the parts came down on the truck, we got stuck into putting the machine back together in its new factory in Sydney. Note the large vacuum box in the corner:

We had to replace a few bits, and repair some damaged parts and cables.
We also pulled the laser’s optics apart and cleaned the mirror and lens, before readjusting and testing it.

Eventually the whole thing was back together and working!
Now there’s just a bit of fine tuning to do before it’s making blinds again.